Have a Husky MZ52 967277401 01 DOM 2013. PTO would not engage blades, did some TS and found bad pull switch. Still had some concerns as I found a spade on the switch that had a small amount of melting with wiring harness. Did a ohms test on clutch and reading was 2.1 ohms. Owner said that blades has cut out a couple of times. Is the PTO clutch on its way to the scrap pile or could the melting just be from switch going bad? Would it help if I run the PTO to heat up and try another ohms test?
Thanks in advance.